Research Article Volume 5 Issue 5
1Lecturer, Department of Apparel Engineering, Bangladesh University of Textiles, Bangladesh
2Executive, Industrial Engineering Department, Fakir Apparels Ltd, Bangladesh
3Trainee merchandiser, Ha-Meem group, Bangladesh
4Executive, Research &Development, Square Fashions Ltd, Bangladesh
5Assistant professor, Department of Apparel Engineering, Bangladesh University of Textiles, Bangladesh
Correspondence: MD. Maruf Hasan, Lecturer, Department of Apparel Engineering, Bangladesh University of Textiles, Tejgaon, Dhaka-1208, Bangladesh
Received: September 23, 2019 | Published: October 11, 2019
Citation: Hasan SMM, Shanta MDMR, Shams AA, et al. Advantages of lean techniques application in apparel industry: case study on knit jacket. J Textile Eng Fashion Technol. 2019;5(5):252-258. DOI: 10.15406/jteft.2019.05.00210
It is proven that by the application of Lean techniques in manufacturing, business can be profited by improvement in the level of productivity and cutting down the processes that is responsible for wastages. In Bangladesh, Apparel industries face a lot of challenges and the most difficult of them is to meet the shipment date. To ensure the products have been manufactured and assembled in due time, manufacturers emphasize on choosing the best method of production process. With the help of Kaizen and 5’s, it is possible to identify non value added processes and eliminate them from the production process. In this paper, we have taken the production data of a knitted jacket and considered the SMV data in two phases, one with the traditional line and the other one is with the implementation of Lean technique to see the differences of SMV data in different stages of production.
Keywords: SMV, lean, kaizen, 5’S, line target, line efficiency
Apparel industries from all over the world faced a great deal of negative impact due to the economic recession back in 2008. And because of this the low cost garments had been urged by most consumer bases from all over the world. Then renowned apparel brands have been forced to cut down the prices to keep their products in the market. They have been shifted their vendors to low cost worker base countries like Bangladesh to keep the competition worldwide. To meet the global challenge, it is really vital to keep the production process in such a way that will not incorporate any types of waste and non-value added process when apparel production process is carried out with lean approach. The terminology is not that much unfamiliar to the manufacturers but they lack in consciousness about the strategic advantages that can be found while lean technique is used in apparel production which is the purpose of our study as well.1–8
Objectives of the Study
For comparing productivity, we collected data from sewing floor of Adury Apparels Ltd, a sister concern of Thermax Group. We considered two lines (traditional & lean line) & differentiate between them. To calculate standard time for each operation, time study is conducted in the shop floor. To do this, a knit jacket is selected as a base line because operations differ from style to style and it is difficult to correlate all these operations of individual styles. After that, at least two operators were selected for each operation so that the difference in timing can be cross checked from the observed data of these two operators. To get better results, each operation time is taken for at least 5 cycles. Once time study is made by collecting raw data the performance rating is given to each operator and actual time is calculated for particular operation. Finally the Personal Fatigue and Delay (PFD) component as an allowance is added on the calculated time and the operation time is standardized. For calculation we have used the following formulas:
Research activities
We use time study to balance these sewing lines which is a part of work study. It implements the use of SMV calculation to identify the points where production has gone below the standard level and the places where the production is above the standard. Then it is balanced to remove bottle neck in order to increase productivity. This system was effective and helpful. Considerable improvement observed by using time study as a line balancing technique changing form traditional layout to balanced layout model. The exchanges of work between the operator & helper caused a significant change in line results of reducing wastage of time, minimum no. of worker and which caused high productivity in the manufacturing process. This balancing process also leads to increased output per day, labor productivity, machine productivity and overall line efficiency.
Lean line operation breakdown (Table 1)
SL no. |
Operation |
No. of workers |
Machine |
Standard SMV |
Actual time Sec(Avg.) |
Allowance (12%) |
Standard Time(Sec) |
Capacity |
|
Manual |
M/c |
||||||||
1 |
Pocket Bone Mark & corner cut |
1 |
MNL |
0.25 |
17 |
1.44 |
18.44 |
195 |
|
2 |
Bone Attach for Pocket |
1 |
SNLS |
0.5 |
32 |
3.84 |
35.84 |
100 |
|
3 |
Body Mark for Pocket & attach pocket |
1 |
SNLS |
0.33 |
18 |
2.16 |
20.16 |
178 |
|
4 |
Pocket Cut |
1 |
MNL |
0.58 |
35 |
4.2 |
39.2 |
91 |
|
5 |
Pocket Top Stitch |
1 |
SNLS |
0.4 |
27 |
3.24 |
30.24 |
119 |
|
6 |
Bone Inside Tack & Pocket Top Stitch Lower |
1 |
SNLS |
0.8 |
51 |
6.12 |
57.12 |
63 |
|
7 |
Pocket Bag Close Both Side(2) |
1 |
OL |
0.4 |
27 |
3.24 |
30.24 |
119 |
|
8 |
Pocket Bag Mouth Close & Scissoring |
1 |
SNLS |
0.8 |
49 |
5.88 |
54.88 |
65 |
|
9 |
Pocket Tack |
1 |
SNLS |
0.35 |
21 |
2.52 |
23.52 |
153 |
|
10 |
Shoulder Join (2) |
1 |
OL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
11 |
Sleeve Cuff Servicing & join |
1 |
OL |
0.4 |
27 |
3.24 |
30.24 |
119 |
|
12 |
Sleeve Cuff Top Stitch |
1 |
FL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
13 |
Sleeve join |
1 |
OL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
14 |
Arm Hole TS (2) |
1 |
FL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
15 |
Side seam join (2) |
1 |
OL |
0.55 |
35 |
4.2 |
39.2 |
91 |
|
16 |
Pannel join at bottom rib (2) |
1 |
OL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
17 |
Pannel mouth TK (2) |
1 |
SNLS |
0.22 |
11 |
1.32 |
12.32 |
292 |
|
18 |
Pannel TS (2) |
1 |
SNLS |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
19 |
Bottom rib join position mark & Rib join |
1 |
O/L |
0.76 |
47 |
5.64 |
52.64 |
68 |
|
20 |
Bottom rib top stitch |
1 |
FL |
0.6 |
35 |
4.2 |
39.2 |
91 |
|
21 |
Zipper cover mark & cover make |
1 |
SNLS |
0.27 |
18 |
2.16 |
20.16 |
178 |
|
22 |
Zipper cover turn & TS |
1 |
SNLS |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
23 |
Zipper COVER ATT |
1 |
SNLS |
0.22 |
11 |
1.32 |
12.32 |
292 |
|
24 |
Zipper piping (2) operation |
1 |
FL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
25 |
Zipper edge fold & TK (2) |
1 |
FL |
0.2 |
11 |
1.32 |
12.32 |
292 |
|
26 |
Zipper ATT - Left |
1 |
SNLS |
0.4 |
27 |
3.24 |
30.24 |
119 |
|
27 |
Zipper ATT - Right |
1 |
SNLS |
0.4 |
27 |
3.24 |
30.24 |
119 |
|
28 |
Collar inner part rolling |
1 |
SNLS |
0.25 |
15 |
3 |
18 |
200 |
|
29 |
Collar inner part mark & join |
SNLS |
0.25 |
13 |
1.56 |
14.56 |
247 |
||
30 |
Collar mark & join |
1 |
SNLS |
0.22 |
12 |
1.44 |
13.44 |
267 |
|
31 |
Back tape piping |
1 |
F/L |
0.22 |
12 |
1.44 |
13.44 |
267 |
|
32 |
BK Tape top stitch& corner fold |
1 |
SNLS |
0.5 |
30 |
3.6 |
33.6 |
107 |
|
33 |
Final thread trimming |
3 |
MNL |
0.5 |
30 |
3.6 |
33.6 |
107 |
|
|
Total |
35 |
|
|
12.77 |
|
|
896.44 |
|
Table 1 Lean line operation breakdown
SMV: 896.44/60=14.94
Standard SMV: 12.77
SMV increased: (14.94-12.77)/14.94x100 =16.99 %
Efficiency% of line: (Total production SMV x 100)/ (No of Operator x working hourx60) = (78x14.94x100)/ (35x1x60) = 55.49%
SMV target fulfillment: (100-78)/100x100%=100%-22%=78%
Basic pace time (B.P.T): Total time/total manpower =896.44/35 =25.61sec
Capacity/hr: 3600/B.P.T =3600pcs /25.61 =140
Traditional operation breakdown of knitted jacket (Table 2)
SL No. |
Operation |
No. of worker |
M/C |
STD. SMV |
Actual Time Sec(AVG.) |
Allowance 12% |
STD. Time Sec |
Capacity |
|
Manual |
Manual |
||||||||
1 |
Pocket bone mark |
1 |
MNL |
0.25 |
17 |
1.44 |
18.44 |
195 |
|
2 |
Bone corner |
1 |
MNL |
0.42 |
27 |
3.24 |
30.24 |
119 |
|
3 |
Bone attach for pocket |
1 |
SNLS |
0.5 |
32 |
3.84 |
35.84 |
100 |
|
4 |
Body mark for pocket |
1 |
MNL |
0.3 |
21 |
2.52 |
23.52 |
153 |
|
5 |
Pocket attach |
1 |
SNLS |
0.58 |
36 |
4.32 |
40.32 |
89 |
|
6 |
Pocket cut |
1 |
MNL |
0.67 |
44 |
5.28 |
49.28 |
73 |
|
7 |
Pocket top stitch |
1 |
SNL |
0.4 |
27 |
3.24 |
30.24 |
119 |
|
8 |
Bone inside tack & pocket top stitch lower |
1 |
SNLS |
0.8 |
51 |
6.12 |
57.12 |
63 |
|
9 |
Pocket bag close both |
1 |
OL |
0.4 |
27 |
3.24 |
30.24 |
119 |
|
10 |
Pocket bag mouth |
1 |
SNLS |
0.8 |
49 |
5.88 |
54.88 |
65 |
|
11 |
Pocket tack |
1 |
SNLS |
0.35 |
21 |
2.52 |
23.52 |
153 |
|
12 |
Care label join |
1 |
SNLS |
0.15 |
6 |
0.72 |
6.72 |
535 |
|
13 |
Shoulder join (2) |
1 |
OL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
14 |
Sleeve cuff servicing |
1 |
OL |
0.33 |
21 |
2.52 |
23.52 |
153 |
|
15 |
Sleeve cuff join (2) |
1 |
OL |
0.33 |
20 |
2.4 |
22.4 |
160 |
|
16 |
Sleeve cuff top stitch |
1 |
FL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
17 |
Arm hole TS (2) |
1 |
FL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
18 |
Side seam join (2) |
1 |
OL |
0.55 |
35 |
4.2 |
39.2 |
91 |
|
19 |
Pannel join at bottom RIB (2) |
1 |
OL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
20 |
Pannel mouth TK (2) |
1 |
SNLS |
0.22 |
11 |
1.32 |
12.32 |
292 |
|
21 |
Pannel TS (2) |
1 |
SNLS |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
22 |
Bottom RIB join position |
1 |
MNL |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
23 |
Bottom RIB join |
1 |
OL |
0.75 |
45 |
5.4 |
50.4 |
71 |
|
24 |
Bottom RIB TS |
1 |
FL |
0.6 |
35 |
4.2 |
39.2 |
73 |
|
25 |
Zipper cover mark |
1 |
MNL |
0.12 |
6 |
0.72 |
6.72 |
535 |
|
26 |
Zipper cover make |
1 |
SNLS |
0.25 |
17 |
2.04 |
19.04 |
189 |
|
27 |
Zipper cover turn & |
1 |
SNLS |
0.3 |
18 |
2.16 |
20.16 |
178 |
|
28 |
Zipper cover ATT |
1 |
SNLS |
0.22 |
12 |
1.44 |
13.44 |
267 |
|
29 |
Zipper piping (2) operation |
1 |
FL |
0.3 |
20 |
2.4 |
22.4 |
160 |
|
30 |
Zipper edge fold & TK (2) |
1 |
FL |
0.2 |
11 |
1.32 |
12.32 |
292 |
|
31 |
Zipper ATT- left |
1 |
SNLS |
0.4 |
24 |
2.88 |
26.88 |
133 |
|
32 |
Zipper ATT- right |
1 |
SNLS |
0.4 |
24 |
2.88 |
26.88 |
133 |
|
33 |
Collar inner part |
1 |
SNLS |
0.25 |
13 |
1.56 |
14.56 |
247 |
|
34 |
Collar inner part mark |
1 |
MNL |
0.25 |
13 |
1.56 |
14.56 |
247 |
|
35 |
Collar 2 part join |
1 |
OL |
0.22 |
14 |
1.68 |
15.68 |
229 |
|
36 |
Collar mark for join |
1 |
MNL |
0.22 |
14 |
1.68 |
15.68 |
229 |
|
37 |
Collar join |
1 |
SNLS |
0.5 |
30 |
3.6 |
33.6 |
107 |
|
38 |
BK tape Piping |
1 |
FL |
0.4 |
20 |
2.4 |
22.4 |
160 |
|
39 |
BK tape TS W/corner fold |
1 |
SNLS |
0.5 |
30 |
3.6 |
33.6 |
107 |
|
40 |
Final thread trimming |
3 |
MNL |
0.5 |
30 |
3.6 |
33.6 |
107 |
|
|
Total |
42 |
|
|
15.43 |
|
|
1013.88 |
|
Table 2 Traditional operation breakdown of knit jacket
Productivity: output/input x100 = 64/100 x100 = 64%
SMV: 1013.88/60 = 16.89
Standard SMV: 15.43
SMV increased: (16.89-15.43)/15.43x100 =9.46 %
Efficiency% of line: (Total productionxsmvx100)/(No of operator x working Hourx60)= (64x16.89x100)/ (42x1x60) =42.89%
SMV target fulfillment: (100-64)/100x100% =100%-36%=64%
Basic pace time (B.P.T) =Total time/total man power = 1013.88/42 = 24.14sec.
Capacity/hr=3600/24.14 =149pcs.
Transportation Analysis (Table 3) (Figure 3)
KPI |
Unit of measure |
Traditional line |
Avg. |
Lean line |
Avg. |
Improvement |
Transportation |
Feet |
351 |
345 |
145 |
143 |
58.55% |
350 |
143 |
|||||
348 |
144 |
|||||
350 |
143 |
|||||
349 |
142 |
Table 3 Transportation analysis
WIP Analysis (Table 4) (Figure 4)
KPI |
Unit of measure |
Traditional Line |
Avg. |
Lean Line |
Avg. |
Improvement |
Inventory/WIP |
Quantity |
815 |
813 |
400 |
400 |
50.79% |
810 |
398 |
|||||
812 |
402 |
|||||
816 |
396 |
|||||
810 |
402 |
Table 4 WIP analysis
Space utilization analysis (Table 5) (Figure 5)
KPI Space |
Unit of measure |
Traditional line |
Avg. |
Lean line |
Avg. |
Improvement |
Utilization |
Minute |
5.77 |
5.55 |
4.62 |
4.52 |
18.55% |
5.6 |
4.5 |
|||||
4.96 |
4.45 |
|||||
5.1 |
4.62 |
|||||
5.55 |
4.6 |
Table 5 Space utilization analysis
Workstation analysis (Table 6) (Figure 6)
KPI |
Unit of measure |
Traditional line |
Avg. |
Lean line |
Avg. |
Improvement |
Work station |
Quantity |
25 |
24 |
11 |
11 |
54.16% |
23 |
12 |
|||||
24 |
9 |
|||||
22 |
10 |
|||||
26 |
12 |
Table 6 Workstation analysis
Defects Analysis (Table 7) (Figure 7)
Defects |
Traditional line |
Lean line |
Seam Puckering |
30 |
18 |
Slipped stitch |
27 |
9 |
Staggered stitch |
18 |
5 |
Thread Breakage |
16 |
8 |
Variable Stitch density |
27 |
11 |
Table 7 Defects analysis
We have used time study to balance these sewing lines which is a part of work study. It implements the use of SMV calculation to identify the points where production has gone below the standard level and the places where the production is above the standard. Then it is balanced to remove bottle necks in order to increase productivity. Considerable improvement observed by using time study as a line balancing technique changing from traditional layout to balance layout model (Table 8) (Table 9).
Topics |
Unit of measure |
Traditional line |
Lean line |
Improvement |
Inventory |
Quantity |
813 |
400 |
50.79% |
Transport Analysis |
Feet |
345 |
143 |
58.55% |
Space utilization |
Min |
5.55 |
4.52 |
18.55% |
Work station |
Quantity |
24 |
11 |
54.16% |
Table 8 Comparing key productivity indicator
Topic |
Traditional line |
Lean line |
Productivity |
64% |
78% |
Line efficiency |
42.89% |
55.49% |
SMV increased |
9.46% |
16.99% |
SMV target Fulfillment |
64% |
78% |
No of worker |
42 |
35 |
Bottlenecks |
2 |
Nil |
Capacity/hr utilization |
149pcs |
140pcs |
Table 9 Productivity analysis
For a jacket, using traditional system our input was 100pcs/hr and output was 64pcs/hr with a productivity of 64%. But when we applied lean system then our input was same but the system was so efficient that we got an increase output of 78pcs/hr. This is a clear indication for increasing productivity. Lack of knowledge, specifically in production systems and resources management of the operations manager of Garments, resulted to the low productivity and efficiency of manpower. The lean manufacturing system is a continuous improvement method; thereby, its implementation helps the company minimize waste, enhance quality of products and definitely create its sustainability. Lean manufacturing tools contribute to the productivity of both workers and the company. The Time Study monitoring system, an output of the study, is an effective and efficient tool to enhance productivity in the entire sewing section, whose benefits extend to the whole organization.
Findings
Though the lean technique is new for most of the apparel industry in Bangladesh but if a industry implement this technique it helps them to increase their overall productivity. Key findings are:
Recommendations
None.
None.
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